Highs and lows in the workshop today
First, I went to look at a drip on the LML I'm going to sell. Realized I'd forgotten the fiber washer on the oil drain. Pulled it off and gasoline pissed out of the crankcase. So I'll be splitting the cases on that one again.
Then, I got back to the fuel leak on the Sprint. Turned out that one of the screws on the fuel tap was loose, so I fixed that up.
Took it out to for a quick test ride and it was struggling to get going, like super rich. One out got going, though, it was its usual self. My initial thought was a clogged idle just, but when I looked in the carb mouth, fuel was spraying insane amounts and making a mess on the back of the cases, so I'm thinking a bad float and/or needle.
I didn't have time to actually check the float, but I'll get there.